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Détail de l'auteur
Auteur David D. Miller
Documents disponibles écrits par cet auteur
Affiner la rechercheCrushed glass-dredged material (CG-DM) blends / Dennis G. Grubb in Journal of geotechnical and geoenvironmental engineering, Vol. 134 n°11 (Novembre 2008)
[article]
in Journal of geotechnical and geoenvironmental engineering > Vol. 134 n°11 (Novembre 2008) . - pp. 1665–1675
Titre : Crushed glass-dredged material (CG-DM) blends : role of organic matter content and DM variability on field compaction Type de document : texte imprimé Auteurs : Dennis G. Grubb, Auteur ; Allen W. Cadden, Auteur ; David D. Miller, Auteur Année de publication : 2009 Article en page(s) : pp. 1665–1675 Note générale : Geotechnical and geoenvironmental engineering Langues : Anglais (eng) Mots-clés : Laboratory tests Recycling Glass Dredge spoil Physical properties Soil mixing Organic matter Field tests Soil compaction Résumé : Trial embankments comprised of crushed glass-dredged material (CG-DM) blends and a 100% DM embankment were constructed to provide the necessary data sets to determine if a moisture content (MC) correction was required for the nuclear density (ND) gauge, as DM may contain a high organic matter content (OC). The MCs of thin-walled tube samples of CG-DM blends collected immediately below the ND gauge were compared to the corresponding ND gauge readings. A direct correlation between the MC data pairings from the tube samples and ND gauge readings showed that the ND gauge was greater than 97% accurate for MCs up to 55% and OCs up to 10% for the CG-DM blends evaluated in this study. However, the MC determined by the ND gauge was underpredicted (not overpredicted) by approximately 2.5%, contrary to theoretical expectations. A comparison of the average MC results per embankment indicated that the ND gauge was generally within 1% of the tube sample values, again on the low side. Interestingly, the rutting of the individual embankment lifts, often used as an informal metric for compaction compliance also was found to be contrary to expectations. The (re)constructed CG-DM embankments of this study were again shown to satisfy local Department of Transportation embankment construction criteria in most cases. En ligne : http://ascelibrary.org/doi/abs/10.1061/%28ASCE%291090-0241%282008%29134%3A11%281 [...] [article] Crushed glass-dredged material (CG-DM) blends : role of organic matter content and DM variability on field compaction [texte imprimé] / Dennis G. Grubb, Auteur ; Allen W. Cadden, Auteur ; David D. Miller, Auteur . - 2009 . - pp. 1665–1675.
Geotechnical and geoenvironmental engineering
Langues : Anglais (eng)
in Journal of geotechnical and geoenvironmental engineering > Vol. 134 n°11 (Novembre 2008) . - pp. 1665–1675
Mots-clés : Laboratory tests Recycling Glass Dredge spoil Physical properties Soil mixing Organic matter Field tests Soil compaction Résumé : Trial embankments comprised of crushed glass-dredged material (CG-DM) blends and a 100% DM embankment were constructed to provide the necessary data sets to determine if a moisture content (MC) correction was required for the nuclear density (ND) gauge, as DM may contain a high organic matter content (OC). The MCs of thin-walled tube samples of CG-DM blends collected immediately below the ND gauge were compared to the corresponding ND gauge readings. A direct correlation between the MC data pairings from the tube samples and ND gauge readings showed that the ND gauge was greater than 97% accurate for MCs up to 55% and OCs up to 10% for the CG-DM blends evaluated in this study. However, the MC determined by the ND gauge was underpredicted (not overpredicted) by approximately 2.5%, contrary to theoretical expectations. A comparison of the average MC results per embankment indicated that the ND gauge was generally within 1% of the tube sample values, again on the low side. Interestingly, the rutting of the individual embankment lifts, often used as an informal metric for compaction compliance also was found to be contrary to expectations. The (re)constructed CG-DM embankments of this study were again shown to satisfy local Department of Transportation embankment construction criteria in most cases. En ligne : http://ascelibrary.org/doi/abs/10.1061/%28ASCE%291090-0241%282008%29134%3A11%281 [...]